Plugging procedures and suspension of drilling operations for injection well KS-7

dc.contributor.authorPuna Geothermal Venture
dc.date.accessioned2015-07-06T23:50:02Z
dc.date.available2015-07-06T23:50:02Z
dc.date.issued1991-02
dc.description.abstract"During the drilling of injection well KS-7, the Puna Geothermal Venture has encountered a high temperature, high pressure zone at depth of 1600'. This zone caused the fluid and steam release on the afternoon of February 21, 1991. Since that time the well has been shut in and is being kept in a stable condition by continuous pumping of cold water into the well bore. During this period equipment and personnel were assembled in order to plug the well. PGV is hereby requesting authorization to execute plugging and monitoring operations that we feel are required to bring the well to a stable and safe condition for the long term. This program is described in the attached document and figures."
dc.format.extent5 pages
dc.identifier.citationPuna Geothermal Venture. 1991. Plugging procedures and suspension of drilling operations for injection well KS-7. Hilo (HI): Puna Geothermal Venture.
dc.identifier.urihttp://hdl.handle.net/10524/47995
dc.language.isoen-US
dc.publisherPuna Geothermal Venture
dc.subjectinjection wells
dc.subjectPuna Geothermal Venture
dc.subjectKS-7
dc.subjectgeothermal wells
dc.subjectwell plugging
dc.subjectwell abandonments
dc.subjectKapoho
dc.subjectKilauea East Rift Zone
dc.subjectKilauea
dc.subjectPuna
dc.subjectBig Island
dc.subjectHawaii Island
dc.subjectHawaii
dc.titlePlugging procedures and suspension of drilling operations for injection well KS-7
dc.typePlan or blueprint
dc.typeReport
dc.type.dcmiText

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